Vertical Mount Filament Drive
Posted: Sun Jul 05, 2015 9:12 pm
Successor to "Bottom Mount".
I began this project when I found that the groove mount can become loose affecting print quality. Several months later I now have a more robust filament drive that exceeds my initial goal.
Nine months, 20+ design changes, and 40+ hours of successful test printing resulted in a filament drive with the following attributes:
* Reduced/eliminated buckling of limp filament: Low friction and low filament-to-PTFE clearance. PTFE guidance of filament from intake to heat break (E3D V.6), or to PTFE insulator insert in MG groove mount.
* Eliminated/reduced internal wrapping of filament around drive gear:
- Reduced radial clearance between filament drive gear and drive body
- Tailored inlet of PTFE guides the filament as it's pushed from drive chamber.
- Form-fitting pressure link replaces bearing.
* More precise control of filament-to-drive gear force: Direct force application via M5 screw and pressure link that are positioned coincident with the center line of the drive gear.
* Probable reduced manufacturing cost and complexity by eliminating bearing and shoulder screw.
* Open drive gear allows monitoring of gear-to-filament engagement. Allows cleaning of gear without removal of filament drive. (At print startup I look for fragments of filament in gear teeth. If present, I clean gear, and increase engagement force with the M5 screw. This has avoided print failures.
* Improved/more efficient ability to service or replace hot end.
I have 40+ trouble-free hours of printing 1.75mm ABS. Looking forward to printing NinjaFlex, Nylon, and other materials.
The present design, although meeting all my performance and serviceability goals, needs to go on a serious diet. I know I can reduce the nose, pressure link, and M5 screw by ~50%. Other ideas would be welcomed.
There will be 5 more photos on the next post
I began this project when I found that the groove mount can become loose affecting print quality. Several months later I now have a more robust filament drive that exceeds my initial goal.
Nine months, 20+ design changes, and 40+ hours of successful test printing resulted in a filament drive with the following attributes:
* Reduced/eliminated buckling of limp filament: Low friction and low filament-to-PTFE clearance. PTFE guidance of filament from intake to heat break (E3D V.6), or to PTFE insulator insert in MG groove mount.
* Eliminated/reduced internal wrapping of filament around drive gear:
- Reduced radial clearance between filament drive gear and drive body
- Tailored inlet of PTFE guides the filament as it's pushed from drive chamber.
- Form-fitting pressure link replaces bearing.
* More precise control of filament-to-drive gear force: Direct force application via M5 screw and pressure link that are positioned coincident with the center line of the drive gear.
* Probable reduced manufacturing cost and complexity by eliminating bearing and shoulder screw.
* Open drive gear allows monitoring of gear-to-filament engagement. Allows cleaning of gear without removal of filament drive. (At print startup I look for fragments of filament in gear teeth. If present, I clean gear, and increase engagement force with the M5 screw. This has avoided print failures.
* Improved/more efficient ability to service or replace hot end.
I have 40+ trouble-free hours of printing 1.75mm ABS. Looking forward to printing NinjaFlex, Nylon, and other materials.
The present design, although meeting all my performance and serviceability goals, needs to go on a serious diet. I know I can reduce the nose, pressure link, and M5 screw by ~50%. Other ideas would be welcomed.
There will be 5 more photos on the next post